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Gold/Mining/Energy : Tusk Energy (TKE) -- Ignore unavailable to you. Want to Upgrade?


To: viper who wrote (655)6/19/1998 10:38:00 AM
From: grayhairs  Read Replies (1) | Respond to of 1207
 
viper,

Agree, but heard that there is also significant vugular porosity (which is very important for the productivity, after "cleanup" of the cement).

Has the flow NOT been continuous since Tues night (~23:00 hours)?? If not, when did they stop the flow?? Are they doing a 4 point test instead of a single point test?? (single is my guess).

Pressure data recovered after the upcoming "lengthy" shut in [which will follow the current/pending flow period(s)] will be analyzed to help define the reservoir size and also to tell them if they should do further acid stimulation of the well.

I believe Well #2 is to spud within 120 days of rig release of the 3-22 well (i.e. by about September 1) under the terms of the farmout agreement. But obviously that requirement could be relaxed by the mutual consent of the parties if there may be prudent reason to do so (possible).

Glad to hear about the 3 putts!!! Now, here's hoping that you 1 putt many times on the weekend. <ggg>

Later,
grayhairs